Just needing to vent. Been chasing an off idle stumble problem for a long time. New plugs. Valve lash done. Air filter done. Fuel filter done. Throttle bodies synched. Timing checked. Compression good. Temperature sensor tested. Finally tracked it down to incorrect injectors installed by PO. Installed correct injectors and noticed immediate resolution. Yippee!!!
As a last step performed the lean drop tuning of the air flow meter and had it set just perfect. Because I'm anal, I decided to wind the bypass screw in and count how many turns it was set at so I could record it in my maintenance records. Started to wind it back out......and it started getting stiff. Turned it back in and started to back it out, and it got stiffer. Squirted some lube down the hole and tried again. Tighter. Disassembled the airbox, took the meter out, sprayed in some carb cleaner,M sprayed in some lube, tried turning again.....now it's locked up solid, about a half turn from fully closed. WTF!!!!
How to go from high to low in about fifteen minutes.
Is this thing now a paperweight, or has anybody been through the same issue and managed to salvage it?