So i bought my k75 with problems.. I think the previous owner was messing with things trying to make them work... I have tested everything electrical many many times. Ignition shows no faults on oscilloscope, cleaned all connections and grounds, have a fuel psi guage, and it stays steady 35+ even when running rough. Replaced fuel injectors, Coolant temp sensor, and many many sets of plugs. They just foul out, ive gone 200 miles on 5 sets of plugs.. Bosch x5dc and NGK bp7ea.
There is a screw that changes how much air bypasses the vane in the air sensor. So today i was running out of ideas because EVERYTHING always tests good, (air temp, vane voltage, coolant temp, tps, hes, signal at the coils..) i decided to pop the rubber grommet and see how far out the screw was.. it was about 1.75 turns out from bottomed out. So i went for a ride and just kept turning it, it seemed to be making the bike run better and better. Mind im still on fouled plug, but i got to 13 full turns out before i ran out of time to keep playing.. so if its 1mm pitch thread then thats 13 mm i have open for air to bypass the vane door. Idk... just seems odd to me, so i figured id ask.
I dont have a sniffer to properly test/adjust it, Sunday i will get some time to play a little more, and i have another set of non fouled NGK to throw in, really hoping this is my issue. Just that going from a carb where 1.5-2.5 turns is the recommended adjustment are, 13 turns seems excessive, i will do more if i must, but perhaps ive already gone too far, and should look for other reasons it is too rich?