« Reply #26 on: June 13, 2024, 10:52:03 PM »
10.8 VDC between Pin 9 and Pin 5.
Wondering if there was some Back EMF that came off of the electrically driven "turbo" that snuck back in to the OEM circuit, that had not been properly back-filtered out from the intake induction, electric motor control circuit? The three 8 gauge (or larger) wires turning the motor were hard wired direct to the battery, so I didn't think noise got in after passing back up through the battery?
However, there was an electric motor control speed signal coming off the green/red throttle position sensor wire (I believe).
What brick circuitry could have been whacked from a possibly spurious signal coming in that way?
The owner immediately previous to me rode it for a while, but parked it when it stopped [details sketchy here], and the shop wanted a lot to investigate [maybe bid a high price to discourage immediate previous owner from bringing it in?]
My previous barn find resurrection (3+ years in a shed after had been running) did not seem this complicated to resolve. :-\

Logged
- North Alabama
- 1985 K100RT very original
Ken
Current: 85 K100RT, 09 DL650, 16 4RT260, 97 XR100, 70 CT70, 06 YFM400
Past Bikes: 86 K100RT, 85 K100RS, 07 SV1000S, 80 KL250, 99 GS1100, 85 K100RT, 86 VFR700, 91 XR250, 95 VLX600, 86 TRX250, 02 GZ250, 83 Z50R, 78 ATC90, 86 XR250, 79 XR500, 72 AT1, 75 YZ360, 78 DT400, 75 DT125, 73 Trail 70